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Abitibi boosts newsprint output and quality at lower production cost with PC-based control system, fieldbus technology. Richard Hatten is the Electrical and Instrumentation Superintendent for Abitibi Consolidated at Steilacoom, just outside of Seattle, WA.
The facility, which dates back to the turn of the century, began producing newsprint in the '40s. The plant's currently operating machine dates back to the mid-'60s. So maintenance, repair, and upgrading equipment are a continual process, and a key part of Hatten's job. In 1999 Hatten oversaw a three-area changeout of the plant's automated control system, to a PC-based digital system, including field-based architecture and FOUNDATION Fieldbus technology. Here, Hatten recounts the system's reduced installation and maintenance costs, and the resultant increased control, performance, and product quality at the mill. The Control challenge Intermittent hardware failures in the wet end of the paper machine had caused 10 to12 hours of shut down time in the month of June alone. The other major issue was correcting improperly implemented control strategies. When a controller was programmed, it did not generate a configuration document, so there was no accurate record of how it was last configured. The only way to tell was to manually scroll through all of the setup menus. Our first challenge was in the reliability of several stand-alone controllers. The wet end cabinet is installed ten feet from the headbox -- obviously a warm and humid environment. The system that pressurized the cabinet had failed and the air conditioning had failed, so the controllers were subject to this adverse operating environment, which contributed to failures. A second challenge lay in some improperly set up control strategies and processes -- specifically on our dry end pulper. These caused weight swings on the wet end of the machine, and often low-consistency stock back through the broke system. If we added water to correct consistency, somewhere down the line, we'd have to take that water back out again. This manual correction invariably threw off the white water balances in the mill. This introduced variability on all the consistency loops that were dependent on a common white water source, compromising quality coming out of the pulper. A third challenge was with the five sets of low volume condensate receivers, which reside in a very high vibration environment. These receivers drain the condensate out of the dryer section of the paper machine. The old pneumatic controls in this area were very susceptible to failure from vibration. As a consequence, we seemed to have a technician in every other day to repair those controllers. Adjustment was difficult and imprecise, and often the job was improperly done. The receiver levels would go unstable, and condensate would either back up into the dryer cans, which reduces drying capacity and slows the machine down -- or they'd run the receivers dry and we'd cavitate and damage the pumps that remove the condensate. The switch to Fieldbus Around February 1999, Representatives from control engineering company PCE Pacific asked me to review Austin, TX-based Fisher-Rosemount's DeltaV system, and its field instrument integration path. We had a considerable investment in intelligent field instruments and an asset management system. I reasoned that if any system was capable of integrating these components, I wanted it. I'd first heard about the DeltaV system among the emerging PC-based control systems a couple of years earlier. But at the time, I didn't believe it offered all the features I wanted in a control system. Now, two years after its inception, I saw a system designed to work in conjunction with the instrumentation that I was putting on the machine today. Implementation Then in September of 1999, we implemented the first phase of the dry end. This was a perfect opportunity to get our feet wet with fieldbus, because it was a stand-alone application with pneumatic controllers and some Fisher valves. We purchased a cabinet and the configuration service. We developed all the graphics and did all the loop drawings and the training documentation for our operations staff. To resolve the ongoing control headache in the area with its high vibration level, we put new fieldbus differential pressure transmitters and valve positioners on the existing valves, all connected via one fieldbus segment going out to all five receivers. In each receiver, the PID control runs between the transmitter and the valve, so we now have five loops running on this one field bus segment. They all execute at about 400 milliseconds, for extremely fast control. The whole system for five level control loops and a serial interface to the PLC for motor control was installed in an eight-hour shift. By then our people had had some training on the new system and we took over the project's configuration. The next area was the steam and condensate system. Here, we put in the cabinet we'd purchased for the condensate receiver. We did all the fieldbus and hardware engineering internally. We did all the graphics, and after some initial fieldbus configuration help, we did most of the control configuration internally as well. The commissioning was that easy. Reduced installation cost Reduced training time Similarly in the wet end, when we implemented the system changeover, we programmed the new system's faceplates to look similar to the old single-loop controllers. So when we made the transition, the operators came in and, with only a couple of hours training, were able to navigate and control the machinery. Reduced downtime Reduced Maintenance Reduced Operating Costs The second thing we've seen -- though not a high cost impact for us -- is big savings in steam consumption, which we have documented at 200,000 pounds per month. The original control strategies were improperly implemented on the thermo-compressors. One of the first things the dry end operators pointed out to me was that we were no longer using any make-up steam. And the reason is simply that the old single loop controllers could not maintain levels and differential pressures adequately by flashing condensate from high-pressure receivers into the next, lower pressure, receivers, thus saving energy. So the mill had been using makeup steam at every set of dryers. It was very simple in the new control system to get the thermo-compressors working properly to provide the flash steam. Improved product quality Improved Control Improved production Conclusion I'm convinced that we've met every criterion we started out to meet in terms of reduced down time, and improved quality and reliability. None of the controllers on the fieldbus side has given us the slightest problem, and we feel that the maintenance cost of the system will be greatly reduced as a result of all the off-the-shelf equipment that comprises the new system. And we fully expect to see a big payback in reduced long-term maintenance of this system. Combine that with the supportability from a local sales force from the vendor, and I think we've got a perfect solution. In summation, the new system enabled our maintenance and operations staff with some tools that allow them to take our paper machine to the next level of performance and quality. With the improvements we've implemented in this old plant, the quality of our product is on a par with any of our competitors. We now have a direction in which to continue cost-effectively increasing our quality and output. Our future steps include continuing to phase out the older generation system, opening further opportunities for variability reduction and production increases we can capitalize on. |
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